Early days it looked quite presentable



Was bought very cheap as the engine was reported blown - turns out it had a bout 2 1/2 gallons of oil in it and 7 blowing exhaust gaskets due to the naff headers.
Engine is a bit of an odd one - its a very late P6 9.25CR after the 10.5's and before the SD1 9.35's - it has SD1 heads block huggers and a list 8007 390 - five speed LT77 and MK1 Capri 1 3.09 axle.Wheels are ultra lite 3 piece Compomotive 14x9.5 rear and 14 x 8 front
But I didn't like some aspects of the build so rather than drive it I took it apart.


And all was not as it should be so I kept going after welding in a few extra bits of metal because there was a definate lack if chassis.


And so it went on

And on

And now at the stage of starting to put it all back together again.



And hopefully in the next couple of months it will be back rolling under its own steam and a lot healthier into the bargain - then the tuning begins
Cheers
Andrew